Post Bake tests
Problems
- FIG5 ion gun filament burned out
- Sample clips on STM stage too loose for good electrical contact, impossible for STM
- Manifold changes needed, existing manifold not optimized, leaking
- evaporator filaments cross wired, not working
Repairs
- FIG5 filament removed, replace with old 04-303 ionizer assembly, almost identical to FIG5 except 3 post rather than 5 post. Send failed ionized to RBD for rebuild
- Stage removed, clips removed, bent to improve sample plate grab, re-installed
- left clip electrically connected to metal "U", right clip isolated
- tricky to get right clip not to short to U since mounting screw passes through kapton washer into U
- changes to manifold, old stuff mostly removed
Bake
- Set for 72 hours, stopped 6 hours early (clock fast)
- bake into turbos, ion pumps open but off
- nano goes to 3e-5 at full temp, constant during bake
- prep 8e-6, slowly drops to 6e-6
- heat off drops to low 8's, with ion pumps running mid 9's, after TSP high 10's
- next day nano 2.5e-10, prep 3.5e-10
Ion Gun
- Brief test of filament before bake, 1 mA emission >> 50 mPa extractor, too much outgassing
- After bake, nano 6e-10, FIG5 pump running
- Turn on 1 mA, grid 150 V, beam 0.5 kV, initially no pressure change, extractor or system
- filament will not come on in standby, must go to etch first. go figure.
- Turn off power supply and software, verify filament continuity, turn back on
- this time it works. probably software. Saved "foundry degass" profile new values
- 150 V grid, 1 mA, 500 V, 100% cond obj
- initial pressure 30 mPa, chamber 1.1e-9, 10:45 am
- pressure exceeds 50 mPa 11:15, gun shuts down self-protect, restart at 0.5 mA, initial pressure 14 mPa
- gun off again after 6 min, reduce emission to 0.2 mA, 28 mPa, later to 0.1 mA at 200 V, emission still > 80 mPa
- pressure peaks around noon, starts slow decline, still 0.1 mA 200 V etch
- 3:45 pm now 1.8 mPa at 25 mA. Note pressure may be normalized by emission current in software, higher current seems to reduce reading
- start to condition HV, pressure about 1 mPa now, 4:45 pm
- OK up to 3 kV, later 5 kV
- extractor still 2 mPa in standby
SEM startup
- connect all cables except detectors, including interlocks and column valve
- switch electronics on to standby, verify column valve closed, switch to on, valve opens
- forgot to start water chiller, SEM water flow error
- start chiller, cycle to standby, restart server, still get flow error
- confirm water is running. Open console whack water flow sensor, right side front behind electronics board, restart, still get flow error
- cycle power 5 times, keep hitting, keep getting flow error
- Remove and dis-assemble and clean flow switch, Gentech International 1 liter/min, closed on flow. No problems with switch.
- Flow is actually low. Run output into bucket, some black powdery crud. Flush with ~ 50 liters water.
- adjust chiller from 2.6 to 3.3 pressure limit (zeiss spec 3.0 bar)
- disable filter change alarm (we have no filter, its optional)
- Now flow switch works
- Now column valve fails. Limit switch does not light. It did on the first run. Loosen tiny set screw so magnetic indicator works
- Close nano chamber gate valve, let pressure rise to mid 8's so zeiss ion pump will start.
- Start gun ramp up
- quick rise to 156 uA, slower increase to 167 and rising
- EHT on 3 kV, gun pressure 7e-9 mbar
- EHT off, 1:45 after gun start, gun 5.3e-10 mbarr, 209.5 uA at 5.02 kV 2.33 A
- next day 5.4e-10, 246 uA
- prior to bake was 223 to 234 back to Jan 2013, around 230 last six months
Manifold
- Ar source, Nano Ar gun, bypass all connected with VCR manifold
- Pump manifold, air lock, gun connection, Ar source, 4.0e-5 after 45 min, let pump over night.
- Overnight 4.1e-7
- apparent small leak in ion gun branch, close valve drops below 4.0, open after few min up to 5
- close manifold valve, no additional drop
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